I have run many jobs on the Nomad and this is the first time it ever stopped in the middle of a job. It said:
ERROR(1): GRBL ERROR: The Motion command has an invalid target. G2, G3 and G38.2 generates this error. If the x arc is impossible to generate or if the probe target is the current position.
I guess I am wondering if anyone else has seen this error or could point me in the right direction. I regenerated the path and will try it again.