I was finally able to get around to cutting something. Made a sim racing hydro brake mount.
First time using anything larger then a 1/8th inch endmill in 6061, 3fl dlc coated Dreanique 6mm. Made and oops and programmed for a 2fl for my chamfer when its a 3fl but im happy with how it came out as a test peice for my machine.
I love the flow control wheel and if I didn’t already have my Cool Mist jr MQL that was like $750.00 I would go this route.
Part of me still wants to make an Arduino controlled syringe system that would work like the pain pumps in hospitals allowing me to have a stepper driven mini linear slider apply precise amounts of cutting fluid to my old hydroponics air blast system with a large syringe and IV tubing. A simple potentiometer stepper speed control code is probably easy to come by.
Are you still using iso-water mix as lubricant? I find that the cool lube 2210al will turn to smoke if I push the feeds above 170 ipm range the machine and tooling can handle it but the heat generated is too much for the fluid to remain stable.
I still use KoolMist + Water + Iso = But for me the best combination of speed and surface finish is about 100ipm. For heavy cuts I also add more mist so its more lubricated, there is a small amount of mist/smoke I assumed it was the iso vapor with water?
I’ve seen a few guys made indexing rotaries that allow rotating the part to cut multiple sides.
Some manual, some controlled by swapping out the Y or X axis from the controller.
IF the part is mounted left to right so it rotates around the X axis, this would be an “A” axis rotary.
I mounted a little Dremel Lathe to my table & zeroed on the centerline of the lathe and used just my X & Z axis to turn a part. This would also be a “A” axis rotary.
Some cuts I made today, I diddnt want to push the machine. Its my third cut in metal on this machine. Facing passes were done with a dlc coated 10mm 3fl 18,000rpm 2000mm/m 0.75mm doc 7mm step over both ways with no changes to lead in lead out.
I think I am going to add a second air blast as I can see where im chip recutting or heating up some on the side that doesnt see air. Finishing pass was .15mm radial full doc with the 10mm 19,000 1500mm/m with a wipe of wd40 on the endmill and face before slicing.
Also I think im gonna up the rpm on my chamfers.
What are you guys doing about chips landing in the linear rails? I am getting so much chip that im stalling the machine when it homes after a cycle because they are caught up in the ways of the rails.
Anyone elses machine get caught on chips and stall alot? Ive had it happen 4 times now and im taking healthy chip loads, its getting aggravating having it happens 90% through a job. I vaccum every time i run and it still does it at random intervals on random axis. Really considering ditching all the electronics and buying real drivers for the steppers.
There are lots of advantages to new electronics but they will not solve that problem. If chips are building up and causing missed steps, you need to figure out how to prevent the chips from building up. A discussion on this might be better as it’s own thread rather than appended to the end of this one.
I have only had that issue if I I didn’t blow off before the machine homed, it went all the way to the end of travel, then compressed a pile of chips. I have not had it happen in normal operation. Unless you’re cutting to the end of the travel of an axis, there is nothing for it to pack up to and stall the machine.
I have a spare 200w hydroponics air pump sitting idle so I’m thinking to add 2 nozzles on the X axis aimed at the ball screw to clear chips off the screw and rails during operation. I also thought about making another half brush guard collar for the spindle because that kept 95% of the chips off my So3 rails but still allowed for chip evacuation and tool change without having to remove it each time.
3fl dlc coated 10mm 18,000 rpm 0.75mm doc and 7mm step over doing some facing.
Was aiming for 10mm thickness
Finished part, its a bracket to relocate my tool setter on the nomad for some mods I’ve done on it (will post a post about it in the unsupported section when its finished). Bracket is v2 because I set a zero wrong on v1 and plunged a .35mm chamfer pass 4mm deep into the hole. Live and learn. Used a 10mm 3fl, 6mm 3fl, 1/8th 2fl, 6mm 3fl chamfer, M6 thread mill and a drag engraver for this part. Please don’t make a deal about the engraving, its just a joke lol.
Was messing around with a 3 flute carbide welded mdf face mill today. Will soon be picking up an indexable insert head and some inserts to hopefully get a full mirror instead of almost one but it still came out nice